Archive for Interior

Bolts, Brakes and Bodywork

After getting the buggy out in the week I was quite in the mood to get working on it again, so we agreed we would get it out over the weekend and see where we had got too and what the next stage was.

Saturday rolled round and we dragged the buggy out, I popped up the shops to get a 1st few we needed, nuts, bolts, washers, brake light switch, fuel line, low pressure brake line. While i was out we got some assistance from a mate who turned up to see how the project was getting on and ended up staying about most of the weekend.

While I fitted up the brake light switch and lines, Simon replaced our test engine wires with proper cables and I gave the body-shell a quick pressure wash.

We checked the chasis over for things that we still needed to do and it appeared to be that time, so before fitting the shell again we thought “Oh what the hell, lets start the engine”, out came the fuel can and the jump leads, after a few tries it fired up with a nice rumble.

A little off the side please...

A little off the side please...

Once this had been done we where really in the mood. So we lifted the body back on and realised that the fiber glass wouldnt quite bolt down as we had forgotten to remove some body mounts designed for the beetle shell, this was nothing the angle grinder couldnt take care of in a few seconds, with that done the body went on and car really started to take shape again.

Seeing as we had fitted the low pressure side of the brake system we decided to add some fluid and see if they worked so we topped it up and bleed the system through. Low and behold the foot brake started to hold the car without the handbrake.

Given that we had wires and pipes in place we decided it was time to bolt the body back down, out came the nuts, bolts and washers and i got to work with the socket wrench.

Starting to take shape again

Starting to take shape again

As the sun started to set I decided to get the steering column out and see what it looked like with it fitted up, after a bit of fiddling it went in and i bolted the dash support in place to hold it up.

Following the success we had on Saturday we got up Sunday morning with a renewed vigor and set to work again.

We found the brakes had gone spongy and after a quick look around we tightened up one of the nipples on the master cylinder as it had been leaking. After bleeding the air out again, we started connecting up the wiring loom. We had previously fitted this into the shell so it just needed plugging into the engine components and did a bit of tidying.

I went back up the shops and bought a battery for the project and some other bits and bobs and we started working on the wiring. We connected up the engine electrics to the wiring loom and checked it was all in the right places.

Then came another big moment when we released we had the wiring all in place to fire up the engine from the dash switches (well by dash switches i may mean wires hanging out). So we moved all the loose tools and sealed a length of spare fuel hose into the top of a plastic bottle, filled it up with some petrol and taped it to the bodywork.

We put a spare battery on the floor as something to rest on, then came the big moment, we flicked the coil switch and touched the wires together, tick, tick, tick, BROOOOM.  The engine fired up quite easily, all be it with a puff of blue smoke from one side.

With the engine running Simon jumped in, dipped the clutch and and popped the buggy into gear and slowly backed it off the drive. This is the 1st time the buggy has moved under its own power since we started the rebuild.  I have this on video and will post it as a seperate entry once i have sorted it out and uploaded it, at this point the camera ran out of batteries so there are no more pictures from todays work.

Having archived this by lunchtime we both had places we needed to go so we tidied up quickly and went out with big smiles on our faces.

Getting back to the project a few hours later we fitted up the rear lights are back on and connected to the loom, I mounted the volt reg in the boot and tidied up the engine electrics, we tested all the lights worked by connecting up there relevent wires in the front of the loom to the battery, we also accidentally tested the horn.

After so much time and effort, I got chance to fire up the buggy and move it around the drive, oh what a feeling.

We finished off the day by wiring up and testing the headlamps, there where a few more jobs we could have done but we have run out of wire terminals.

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Quick Renders

Just a few quick renders from the CAD model I have been working on. First in plain metal as we will be getting it made. Then a 2nd render in carbon fiber just to see what it would look like.

Metal Render

Metal Render

Carbon Fiber Render

Carbon Fiber Render

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Slime and Drawings

Robin was back round to give us a hand with some fiberglass today; one hole needed patching from when we got the shell, the other hole we made removing some of the old parts when we dismantled the car.

Floating Body

Floating Body

We started by lifting the body up onto the rack we used for the floor pan welding and a work bench so that we could get underneath it and so that we didn’t have to bend over onto the floor to work. Simon and Robin scrapped most of the old rubbish off the inside of the shell and around the holes to be filled, following this they patched the holes with wire mesh and repaired the fiberglass.

While Simon and Robin worked on this I started work on a technical drawing for the dashboard following the graphical design Simon made last night to show what we wanted it too look like. I have started building it in CAD so that we can produce accurate plans. The reason for this is that we are looking at getting the plate stamped out instead of trying to cut it out ourselves, this will be a quick and easy way to make it look professional and get everything in exactly the right place.

Here is the cutting diagram as it currently stands, it may well need some adjustments before it can be pressed but i will work on them once i get a response from the companies I have approached to do the work.

Technical Drawing

Technical Drawing

Here is one of the patched holes: (Better pictures to come tomorrow when it’s light)

Patched hole

Patched hole

Next steps:

  • Build a basic boot (wood only no treadplate for now)
  • Get the wiring loom in place suspended in the shell
  • Clean the body up some more

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Dashboard Design

Last night we spread the wiring loom out on the floor in the house. Then with a roll of masking tape, a pen and the wiring diagram we labled both ends of every wire.

We have also decided on the new layout for the dashboard; the old layout was a mess and looks like the dials and buttons have been chucked at the dash while blind folded.

Dashboard Design

New Dashboard Design

The dials/lights are as follows left to right:

  • Volts, Amps, Oil temp, Oil warning light, Oil Pressure, Revs, Speed, and Fuel
  • On the far right hand side is a clock, as well as a plague we’re going to have there.
  • Switches underneath are for main power, push button start, ignition, aux, hazard lights, headlights, dip/high-beam. All of these have a telltale light underneath them as well.

From this mockup I have just started work on a technical diagram of what needs cutting and where.

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Day 9 – Planning/Slacking

Corbeau Clubman V2 Bucket Seats

Corbeau Clubman V2 Bucket Seats

Jon’s off getting his car valeted today (tart) so I’ve spent the day researching and planning. I’ve added links on the right to our photo sets on Flickr, and to my list on Kaboodle of all the kit we’re going to need to buy. I’m expecting this list to increase a lot.

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