Time To Get Greasy

After all the work getting the cables and pedals installed yesterday I realised we had not greased the throttle cable, so I took this out and gave it a good greasing, lucky its not the cable that is inside the center tunnel or it would probably have remained not greased. While i had the grease out I removed the bar that runs through the pedals that operates the accelerator and greased this too, this has made the pedal movement a lot smoother and easier.

Well the time came to do one of the jobs I really had not been looking forward too, but for a lot of things the hardest looking jobs turn out to be fairly easy and the simple stuff takes forever. With that thought in mind I set about removing the wheels and hubs to change the wishbone arm ball joint covers.

My previous thought proved not to be the case, It looked like a hard and annoying job and was both hard and annoying. It probably took a good 1/2 day to change these while doing other stuff and working out how and where things go.

3 Legged Puller and Blow Torch

3 Legged Puller and Blow Torch

Getting the bolts undone was a lot easier then expected and removing them was not too hard with the aid of a long bar to leaver them out.

Once the wheels and hubs where out of the way the real fun started, the top ball joints looked like they would be harder but proved to be easy by comparison, once with got the eccentric camber adjustment things off, these where seized onto the ball joints and needed to be removed to get the new covers in place. Removing these required a 3 leg puller and a large dose of flame, but once off the new covers where not to hard to grease and refit.

The bottom ones that started out the day looking easy turned out to take more time then anything else, getting the new covers into the correct place and seated was just so much harder than it should have been.

Now the bigest problem stopping us reassemble the font end and being able to put the car back down on its wheels is the stuck bolt that sheared off in the steering arm yesterday.

Spot the new part?

Spot the new part?

The last part of the brake system that needed to be replaced was the drivers side flexible brake line as this was leaking when we got the car. This line was also compleatly coroded onto the old solid line and the brake drum, the heads on both ends just disintergrated when we tried to undo them, this was quite easy to fix as the line fits into the back of the piston which can be removed from the hub. We took the pair out as one and replaced the piston, a new line is on order and will be with us tomorrow morning. Once we had the new brake parts in place inside the wheel hub we hooked up the last of our new solid lines and as soon as the flexy line is connected tomorrow that will have ticked another job off the list.

Simon has gone to Phil’s (The Phil that helped us with the welding) to try and fix the current arm, he will post an update when he is back with the freshly fixed part.

The next really major task to come is to build the new wireing loom, this is going to be a whole different set of challenges.

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Going, Stopping, Turning the Rebuild Continues

We have both had this week off work so have been getting down to some more of the bits and bobs that need doing. We are slightly ahead of our planning so that’s a bonus as the original plan doesn’t allow for any slacking over the winter and Christmas.

Since the last update we have done a whole load of stuff and things are starting to take shape again.

Top Mount

We have removed the front and rear suspension, changed the top mounts as the old ones where perished and disintegrated as we took them off, then refitted them with nice new ones and returned them to the chassis.

Thanks need to go to Pete, a fellow VW fan, for lending me his spring compressors the other week, needed them again for the suspension work on this.

We have fitted, modified, built and generally re assembled the pedals and all the linkages for them. This involved a lot of swearing as they where not the easiest of things to get back in place, then only to find they had to come in and out a further 4 or 5 times to get all the bits the right shape and in the correct place and then finally connected up and bolted down.

We had to adjust the mounting for the brake master cylinder as we bought a LHD one for 1/3 of the price of the RHD ones.

This is all well and good but the brake pipes come out into the center tunnel.

Master Cylinder

Master Cylinder

So we have spun it around 90 degrees and refitted it. This allowed us to get away with using the cheaper part but might make filling and bleeding a bit more tricky.

We have made up and fitted new brake solid lines as the old ones got chopped up and/or lost and wouldn’t have gone too our newly mounted master cylinder anyway.

We have replaced the throttle and clutch cables and refitted them to the new pedal linkages, and adjusted them roughly into place.

http://farm4.static.flickr.com/3012/3010580686_17c7e25dfa_m.jpg

Pedals, Master Cylinder and Brake Lines

We ended up with some new toys as well, we needed a second workbench and some more sockets and some grease so off we went shopping, came back with a new bottom cabnet tool chest and a heap of other stuff

You wouldnt know I didnt have the tool chest before as its now full up with stuff that just seemed to be floating about.

We have removed the tie rods and cleaned them up, replaced the rubber ball joint covers and given them a good re-greasing.

Getting the split pins and the nuts off was not too hard but we had to get out the good old blow torch to losen the pins off and then a swift smack with a mallet to remove them. This might have caused a small fire as the grease that had leaked from the torn ball joint covers went up.

Flame

Flame

Only problem is that in the process of taking the arm off the bottom of the steering box the bolt sheared off inside the arm, I have spoken to www.vwheritage.com who have been nothing but helpfull throughout the whole project and they imparted some bad news on us. The arm is not in production anymore and can’t be bought new, so we either need to repair ours or find a 2nd hand one (or forge our own :D – Simon).

Steering Arm With Snapped Off Bolt

Steering Arm With Snapped Off Bolt

So if anyone is breaking an old beetle we need a new arm now, or if someone knows how to get good and proper seized sheared off bolt out please let me know.

Next on the list is to replace the wishbone ball joint covers, and this is a job I am not looking forward too.

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More Parts Have Arrived

While sitting at my desk minding my own business today I got a call from the receptionist at work to say a heavy box had been delivered for me.

Yup that would be the buggy parts I ordered. They don’t look like much in the box but should help get a lot of little jobs done.

Parts Shipments

Parts Shipment

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Bulk order of parts

Jon is ordering the following parts tomorrow ready for fitting next week:

  • Master cylinder (Brake system)
  • Accelerator Cable
  • Clutch Cable
  • Accelerator pedal assembly
  • All the rubber bits for the steering etc

I’m gonna try and pick up some underseal ASAP as well tomorrow, then I can do that one evening this week.

Posted a poll as well as we can’t decide what color to paint it. I’ll leave that page up until we make the choice.

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We finally have floors!

We finally decided to pull our thumbs out and do some more work, the new floors have been sat in the garage for like a month or so. So we got up fairly early on Saturday morning and cleared the driveway shortly to be joined by this updates guest star. Simon’s fiance’s dad just so happens to be a welder and also loves boys toys so the buggy is right up his street.

Jacked...kinda

Jacked...kinda

After getting the front wheels off and the buggy lifted up onto a makeshift framework we had in the garden, we set to work on cleaning off the remaining dirt.

Phil brought out his gas welding set and a length of steel right angled plate and the real work began. With Simon and Phil shouting out measurements, I cut some plates and angle bars to remake the missing front sections. Rebuilding these took most of the morning and a steady supply of cups of tea. (Cheers Rachel!)

After stopping for some chip shop lunch we cracked on with getting the new floors in place and started the welding, this is where we ran into problems.

Fixing the front of the pan in place

Fixing the front of the pan in place

The new floors are nice new thin metal and the original center tunnel is heavy steal, there was just no way we could get enough heat into the center tunnel with the gas torch to weld them together before the metal of the floor pan melted away. Next we tried the arc welder, this is a unit I picked up cheap a few weeks back but this had the same sort of problems, with the thicker rods the arc just blew the floorpan metal away and with the thin ones there wasnt enough power to heat the tunnel.

While all of this was going on Simon disassembled the front right brake drum and hub to find out why it was so stiff, after adjusting the brakes and a bit of wiggling and testing it now spins a lot better.

By this point it was starting to get on towards dusk and we wherent getting anywhere with the welding kit we had, so I pulled out the phone and made another quick call. Knowing that Edd (Previously mentioned for the lending of his airline and generator) had just bought a MIG set, I scrounged and mangaed to borrow this while he was out.

So with a bodged uplighter + flood lamp combo and the flash from the welding sets lighting up the drive we carried on into the darkess.

Working into the night

Working into the night

Once simon had finished getting his technique down the welds where going in quick and steady. Top it off with a good brusing down then a coat of hammerite over all the bare metal and the floors are in and protected.

Seeing as its nearly payday and we both have next week off work we are planning on getting on with the little bits and bobs that need replacing and rebuilding before the body goes back on.

Simon knows a man who knows a man who happens to work in a body shop as a painter so is in the middle of aranging to get the car resprayed. (That means you Steve!)

The Flickr gallerys for me and Simon have both been flooded with pictures, and Have a fantastic slapped together video of the days efforts:

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Tiny update

Ordered the floor pans, should be here by Tuesday. Then as soon as the weather clears up it’s welding time.

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Photosynth Buggy

I thought I’d use the buggy as a test subject for the newly released Microsoft Photosynth. Gives you a nice 3D view of the buggy with only minimal effort on my part :)

Click here is the result (Requires Windows, sorry Mac/Linux peeps):

Click to view the buggy photosynth

Click to view the buggy photosynth

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Engine and Hammer Time

Best couple of days yet – by a long way. Well, possibly not as good as the day we first went to see it before buying the buggy, but it ranks pretty high!

Last cutting and grinding

Last cutting and grinding

Yesterday we did the last bits of cutting and trimming with the angle grinder (Which is lucky, because we also broke the angle grinder!). We got the little bits around the pedals removed, and cut away some old brake line sections. With a borrowed angle grinder we smooth out the burrs from the floor pan welds.

Next we moved onto attacking the entire thing with the wire brush attatchment for the drill. This is, by the way, clearly the best tool you can ever buy for 49p! We used it to get into all sorts of tight places in the transaxle, the suspension, and the front member. With the help of the drill and a traditional hand held wire brush, the last of the (fixable) rust was gone. YAY.

Pressure washing

Pressure washing

To get off the remaining dirt and rust we got out the pressure washer and blasted it all back. At this point, we found new colour on some parts we hadn’t yet seen, and discovered some newer components which had been replaced. We also washed and scrubbed down the body inside to get out the mud, mould and plants that were living there.

To make sure we could do it, we decided to test the engine. It took about 30 minutes with the wiring diagram and some creative use of old cables we had to rig the engine up to run. In the absence of a battery, we had to start it from my car. In the absence of a fuel tank, we dunked the line in a fuel can from my old buggy :) This was a very worth while activity, as it’s massively rejuvenated our want to work on the thing! She sounded beautiful – see the video at the end.

Hammerite the front member

Hammerite the front member

Last task of the day was to seal what we’d cleaned up before we started welding on the floor. We popped to Andersons and picked up a large-ish tin of hammerite – silver hammered look. This was so easy to apply it shocked us. You could litterally slap it all on and it would stay there! The chassis is now looking silver everywhere it should be, and ready to receive floors.

Next steps:

  • Purchase and weld in place new floor pans
  • Investigate/Repair/Replace brake master cylinder
  • Build brake lines

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Day “lots” – Floor be Gone

Well it has to be said, we have been slacking – it’s over a month since we last posted.

With both of us about and some good weather it was long overdue a session working on the buggy, so out it came and we got back to work.

I have got time off next week so we decided to get stuck into the other floor pan and get it ready to spend some time cleaning up the welds and possibly putting the new floors in. I have found a mate selling an arc welder cheap so as soon as I have some cash I will grab that.

Things hit a small hitch today as we realised we may need to replace more than we planned, that and as we haven’t yet ordered any new parts we are going to be a little stuck next week. But there is always plenty to get on with.

So I started by taking out the last bit of the floor pan under the pedals and then the pedals themselves. Simon made much shorter work of cutting out the passenger floor than the drivers, once the majority of this was cut out I started up the airline and took out the edge and all the spot welds.

All in all this side took less than 2 hours to get out so I don’t think that’s bad going.

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Day 31 – Back to Business

It’s been a while since we did any work as we’ve had quite the hectic week. We’re back on task now though, and the next step is to get the last of that floorpan out. We wheeled the buggy around onto the driveway and powered up the airline. As it’s being so long I’ve even got some video for you.

Getting the floorpan edge off it’s welds is supposed to be simple, and for once, it was! We simply wedged the air chisel into the welds and hammered them till they came out. It was then a case of rolling the metal along moving from one weld to the next. We got 3/4 through removing the first pan in about an hours work which isn’t bad going. Time to get the new ones ordered and ready to weld into place.

We also will need a new copper brake line made up because the old one needed braking away to get the welds out – it ran right on top of them. It does look like whoever last changed the pans went a little over the top with the spot welds. There is meant to be one every 6-7 inches, we were finding them every 1-3 centimeters :S

There is a few new photos in my Flickr set

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